@@ -1618,25 +1618,35 @@ static int omap8250_suspend(struct device *dev)
{
struct omap8250_priv *priv = dev_get_drvdata(dev);
struct uart_8250_port *up = serial8250_get_port(priv->line);
+ int err;
serial8250_suspend_port(priv->line);
- pm_runtime_get_sync(dev);
+ err = pm_runtime_resume_and_get(dev);
+ if (err)
+ return err;
if (!device_may_wakeup(dev))
priv->wer = 0;
serial_out(up, UART_OMAP_WER, priv->wer);
- pm_runtime_mark_last_busy(dev);
- pm_runtime_put_autosuspend(dev);
-
+ err = pm_runtime_force_suspend(dev);
flush_work(&priv->qos_work);
- return 0;
+
+ return err;
}
static int omap8250_resume(struct device *dev)
{
struct omap8250_priv *priv = dev_get_drvdata(dev);
+ int err;
+ err = pm_runtime_force_resume(dev);
+ if (err)
+ return err;
serial8250_resume_port(priv->line);
+ /* Paired with pm_runtime_resume_and_get() in omap8250_suspend() */
+ pm_runtime_mark_last_busy(dev);
+ pm_runtime_put_autosuspend(dev);
+
return 0;
}
We should not rely on autosuspend timeout for system suspend. Instead, let's use force_suspend and force_resume functions. Otherwise the serial port controller device may not be idled on suspend. As we are doing a register write on suspend to configure the serial port, we still need to runtime PM resume the port on suspend. While at it, let's switch to pm_runtime_resume_and_get() and check for errors returned. And let's add the missing line break before return to the suspend function while at it. Fixes: 09d8b2bdbc5c ("serial: 8250: omap: Provide ability to enable/disable UART as wakeup source") Signed-off-by: Tony Lindgren <tony@atomide.com> --- drivers/tty/serial/8250/8250_omap.c | 20 +++++++++++++++----- 1 file changed, 15 insertions(+), 5 deletions(-)